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Engine Torque Bushing: How hard could this be?

Like nearly every Ford Freestyle on planet earth, the Bushing in the upper engine

Torque mount is broken
torque mount was broken.  Reading some other forums, this failure seems to dog cars with the V6 3.0 mill found in my ride.

What's the purpose of this part? The engine in a car will "twist" in the direction of the crank shaft's spin.  Since this engine's crank spins in clockwise motion, the engine will twist in the direction of the front bumper.  The engine mounts resist this force, and, in the case of this car, there's two mounts (one above the engine, one below) designed to further resist the torque so the engine stays under the hood and delivers power to the wheels to move the vehicle.

Two approaches

While not necessary for the safe operation of the car, evaluating the options for repair made sense.  After a little research, two possible solutions made themselves apparent:
  1. Purchase a new torque arm with bushing
    This costs about $120.  The torque arm would contain a new bushing, the work would involve swapping out the old arm for the new.
  2. Purchase just the bushing
    This costs about $15.  I would have to remove the old bushing and replace it with the new one.  I could leave the torque arm attached to the engine and try to press in the part in situ thus saving some work.
Guess which one I picked? The cost was one reason, the other being that the torque arm was in good repair, so why buy another?  How hard could it be to press a new bushing into place?  I don't have a press, but I could at least use some clamps, screws and wood to force the bushing into place.

Removing the old bushing

Can't replace what you don't remove.  So first order of business: extracting the old bushing from the Torque Arm.  I started by removing the 13mm bolt running through the torque arm connecting it to the body of the car. Then it was easy to see the poor condition of the bushing. What you can't see clearly in the first picture is that the part of the bushing holding the bolt was completely separated from the rest of the part.

After I removed the bolt holding things in place, the middle of the bushing just fell out onto the top of the engine, I grabbed this part and took a picture of it on the bench.  

Cutting out rest

Using a hacksaw, I flipped the blade upward and threaded it through the now evacuated bushing.  I carefully cut in two places, making sure not to cut the mounting itself.  Using a flathead screwdriver, I pushed down between the cuts and the old part collapsed and fell out.  Not wanting to damage the arm itself, I didn't cut all the way through the metal of the bushing, so that's why I needed a little extra help from the screwdriver to relive the pressure.

Installing New bushing

The plan was to leave the torque arm in place and using some grease and pressure, press the new busing into place.  This did not go well... it was a learning experience!  I'll ruin the suspense: I did, eventually, finish this project, but not in the way I expected at the start.

Attempt 1: Oil Filter Socket plus Wood with Bolt and Nut

Expectation: Using a oil filter socket to hold a bolt and send the force to the edges of the fitting, I would "wind" the bolt to draw the part into place.  The leverage from the bolt and nut would produce enough force to accomplish the job

Reality: The bolt wasn't sturdy enough and bent under force when wound, the threads failed, causing difficulty removing the nut when this didn't work.  Not visible in the picture was the deformation of the washers.  It was also very difficult to keep the oil filter socket in place when under low compression. After about an hour, zero progress.  Interestingly enough, there was no damage to the oil filter socket.  It was necessary during my Toyota-owning days and even though the car's gone, the few tools I needed just for it remain in the garage.

Lessons learned: Not sure what to expect for a first attempt, but I think I didn't get enough clamping force from the bolt/nut despite having a good way to distributing the force the edges of the bushing.  Will need to improve method of delivering force, bolt/nut good idea in theory, implementation left much to be desired. Just like the Toyota, the oil filter socket was tougher than it looked.

Attempt 2: Hot & Cold with Metal Braces and C Clamp

Expectation: I would warm the arm (thus making it slightly larger) and cool the
bushing (therefore, making it slightly smaller).  Once in their expanded and shrunken states, I would then be able to force the bushing into place with less force.

To apply force, I used a c clamp that could exert 11,000lbs of force (that's what the tag said) and I used a metal shelf upright so I could apply force across the outer edges of the part, making the best use of the squeeze created by the c clamp.  Why a metal shelf upright? Because that's what I had.


Making the bushing cold was no problem, I put it in the freezer overnight.  Heating the torque arm was another story.  I don't have an acetylene torch, but I do have plumbing tools and a few canisters of MAPP gas (which burns a little hotter than propane, but not much), but I was worried about stressing the metal, so I used my wife's heat gun.  Not getting the part warm enough, I covered it with some insulating material (yes, a bath towel) and let things run for twenty or so minutes. 

Reality: After some effort, we did get a little of the bushing into place.  However, the c clamp couldn't deliver enough squeezing force to do the job.  I used some lubricant on the threads of the clamp so it word turn easier, but that didn't make much of a difference.  As I was turning the clamp, it wasn't moving the bushing much, but the threads were advancing.  That's when I noticed I was actually twisting the clamp itself.

Lessons Learned: The heating and cooling really didn't make much of a difference.  The c clamp I think did the work here, just not enough force to push the bushing through. Under the pressure, the c clamp also failed, twisting enough so that it doesn't function well as a c clamp any more. Also: maybe the lubricant helped?

Attempt 3: Better Metal Braces with Improved C Clamp plus Bolt and Nut

Expectation: A better clamp and clamp supports would distribute an increased 
clamping force better,  resulting in the part being seated in the torque arm.

Before...
Reality: I dropped Lowes and picked-up some metal framing pieces and a few class 5 bolts  (attempt 1 was using a puny class 3 bolt) and nuts. The "class" is a rating of the shear strength of the bolt.  Using the ever handy Pocket Ref (just get one) I see that I could get about 1500 lbs of clamping force with the bolt and the clamp was rated at another 1500 lbs.
... after
I tried just the bolt and washers first.  These worked better in that they warped the metal and made the extra wood supports groan, but the bushing barely moved.  So I added the clamp and got maybe the best result, pushing the part in about 10mm.  Then all progress stopped and I noticed the clamp was twisting again.

I used an socket extension to get more leverage to turn the c clamp, this worked well until I bent the tool's handle.  The handle bending should have alerted me that I was exceeding the clamping power of the tool, but I just kept going anyway, as I was determined to make this successful.

Another bent c clamp
Lessons Learned: The class 5 bolt made a big difference, it didn't warp (much) and was able to put enough pressure on bushing that it was pressed into the part much more than the prior approach.  Still even with metal bracing, enough force couldn't be created to seat the bushing.  The body of the c clamp didn't twist, but I used 3/8 extension to increase the turning force on the handle (or tension bar) and this seemed to be the weakest link.

Attempt 4: 12 Ton Shop Press

Expectation: a 12 ton press would create enough force to push the bushing into the torque arm. I would need to remove the torque arm because the press is something that could not be positioned over the engine.  This would be much easier because, I would be doing the job the right way. Doing things "the right way" is easier, at least most of the time, in certain circumstances, under most conditions, forgoing extenuating situations.

Hard to reach bolt...
with Locktite
Reality: Removing the torque arm was a bear.  Three of the four 13mm bolts were readily accessible, after removing the battery, air intake, air filter box and the throttle.  The last bolt was behind the engine and tilted slightly downward, making it very difficult to reach.  A universal joint on the socket didn't help because it needed to bend to less than 90 degrees.   Plus the bolts were held in with some blue Lock-tite, so I needed even more torque to break the initial grip, while pushing in on the bolt so the socket didn't cam out.  Reaching the bolt with the breaker bar, I was able to break the bolt free, then I could reach with the ratchet, but just barely.  I could position my ratchet just enough to get two clicks per turn.  The ratchet has 36 teeth @ 10 deg per click, so each 360 deg turn of the bolt took 18 back and forth motions.  The Lock-tite prevented my from spinning the bold with my fingers once loose, I needed the extra leverage from the socket handle to overcome the friction of the bolt's threads. Going was very slow, I wasn't happy, but, eventually, the arm was free.

Before pressing
Parts removed from engine for access
A buddy from work pressed in the bushing with about 10 minutes of effort.  I was complaining to my work mates about my lack of success and he offered to lend a hand, as his garage was equipped with a floor press.  I don't have pictures of the work in progress, but I do have one with the new part installed before I put the torque arm back on the engine.
Ready for install

Lessons Learned: I thought this was going to be an "easy" project.  The parts were cheap ($15) and what I needed to replace was sitting right there in front of me, no digging through the engine necessary.  Not so.  Just because it looks "easy" doesn't mean it will be actually easy. 

The Result

The engine feels better when pressing the gas, not necessary faster, it has a more solid feeling when accelerating.  When I got the car, it felt like the acceleration was sluggish -- but when I did this job, I also cleaned the throttle body (more on that later...) so attribution of this change to just the mounting wouldn't be good logic.  Maybe I've prevented the engine mounts from failing prematurely, but that's just a guess.

Had I known it was going to be this difficult, I would have just ignored the engine mount and put my efforts elsewhere.  The cost wasn't that much, it was the time (this took over a week to completely fix) involved to make the repair I found to be frustrating, as there's other things in need of attention.


This post first appeared on 500 Dollar Car, please read the originial post: here

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Engine Torque Bushing: How hard could this be?

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